<?xml version='1.0' encoding='utf-8'?>
<oai_dc:dc xmlns:dc="http://purl.org/dc/elements/1.1/" xmlns:oai_dc="http://www.openarchives.org/OAI/2.0/oai_dc/" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.openarchives.org/OAI/2.0/oai_dc/ http://www.openarchives.org/OAI/2.0/oai_dc.xsd">
  <dc:creator>Paul A. Hsieh</dc:creator>
  <dc:date>2011</dc:date>
  <dc:description>When the Macondo well was shut in on July 15, 2010, the shut-in pressure recovered to a level that indicated the possibility of oil leakage out of the well casing into the surrounding formation. Such a leak could initiate a hydraulic fracture that might eventually breach the seafloor, resulting in renewed and uncontrolled oil flow into the Gulf of Mexico. To help evaluate whether or not to reopen the well, a MODFLOW model was constructed within 24 h after shut in to analyze the shut-in pressure. The model showed that the shut-in pressure can be explained by a reasonable scenario in which the well did not leak after shut in. The rapid response provided a scientific analysis for the decision to keep the well shut, thus ending the oil spill resulting from the Deepwater Horizon blow out.</dc:description>
  <dc:format>application/pdf</dc:format>
  <dc:identifier>10.1111/j.1745-6584.2011.00813.x</dc:identifier>
  <dc:language>en</dc:language>
  <dc:publisher>Wiley</dc:publisher>
  <dc:title>Application of MODFLOW for oil reservoir simulation during the Deepwater Horizon Crisis</dc:title>
  <dc:type>article</dc:type>
</oai_dc:dc>